Carl Wiese
Member
For those of you who have followed the thread on the bb in the IHSTO forum, but no longer visit that site, I figured you deserved an update!!
About a month ago Dad informed me he didn't like the isky lifters we had used when we rebuilt the engine. I wasn't too happy with them either, with two of them being bad out of the box! It seemed as we still had lifterer issues, so Dad had taken it upon himself to buy me a set of replacement lifters, clevite this time!! So, last month we pulled the valve covers off, removed the rocker arm assemblies and push rods and replaced all the lifters. We did it the hard way, with a magnet!! Needless to say after much patience and trial and error we got all 16 out and the new 16 in.
I am pro at taking the valve covers off this engine, as I had done it many times before while we were trouble shooting before the rebuild. I knew exactly what needed to be removed or loosed to get them off. One thing you have to do is loosen the alternator and alternator/ac bracket. While I was under the truck working on the alternator I noticed the clear fuel filter we had installed was about 1/2 full with gunk!! On closer examination it turned out to be the fine central oregon dust we all love. The tank I though was okay, turns out it's been full of crap this entire time, and can most likely be blamed for all the "carb" problems I have been having over the past year.
So, tonight we put that theroy to the test. We rigged up a old electric pump Dad had, ran gas out of a clean gas can, with clean new fuel line. We pump gas up the carb and turned it over a few times. I gave it one shot of gas, Dad closed the choke and we gave it a try. The truck fired right off and just ran!! It ran great!!! No misses, no wildly bouncing fuel pressure nothing, it just ran!!
Now something really odd happened. We had turned the truck over for about 5 second before we pumped gas to the carb, then we ran it for about 10 second before gas spurted out of the old fuel line. I had disconnected it from the manual fuel pump but had not plugged it! It took all that time, when it should have been pumping to finally pump.
So, we can honestly say now the problem has been fuel delievery to the carb, not the carb itself. Months and months ago Mike, had hypothesised this and we decided it was going to be the trouble shooting tact to take. His idea was get good fuel and fuel pressure to the carb and go from there. In a few weeks I'll be back at Dad's house to drop the tank, clean it and put in new fuel lines and filters, then go from there.
Needless to say I am really happy!
About a month ago Dad informed me he didn't like the isky lifters we had used when we rebuilt the engine. I wasn't too happy with them either, with two of them being bad out of the box! It seemed as we still had lifterer issues, so Dad had taken it upon himself to buy me a set of replacement lifters, clevite this time!! So, last month we pulled the valve covers off, removed the rocker arm assemblies and push rods and replaced all the lifters. We did it the hard way, with a magnet!! Needless to say after much patience and trial and error we got all 16 out and the new 16 in.
I am pro at taking the valve covers off this engine, as I had done it many times before while we were trouble shooting before the rebuild. I knew exactly what needed to be removed or loosed to get them off. One thing you have to do is loosen the alternator and alternator/ac bracket. While I was under the truck working on the alternator I noticed the clear fuel filter we had installed was about 1/2 full with gunk!! On closer examination it turned out to be the fine central oregon dust we all love. The tank I though was okay, turns out it's been full of crap this entire time, and can most likely be blamed for all the "carb" problems I have been having over the past year.
So, tonight we put that theroy to the test. We rigged up a old electric pump Dad had, ran gas out of a clean gas can, with clean new fuel line. We pump gas up the carb and turned it over a few times. I gave it one shot of gas, Dad closed the choke and we gave it a try. The truck fired right off and just ran!! It ran great!!! No misses, no wildly bouncing fuel pressure nothing, it just ran!!
Now something really odd happened. We had turned the truck over for about 5 second before we pumped gas to the carb, then we ran it for about 10 second before gas spurted out of the old fuel line. I had disconnected it from the manual fuel pump but had not plugged it! It took all that time, when it should have been pumping to finally pump.
So, we can honestly say now the problem has been fuel delievery to the carb, not the carb itself. Months and months ago Mike, had hypothesised this and we decided it was going to be the trouble shooting tact to take. His idea was get good fuel and fuel pressure to the carb and go from there. In a few weeks I'll be back at Dad's house to drop the tank, clean it and put in new fuel lines and filters, then go from there.
Needless to say I am really happy!