Rusty Scout
Member
To make a long story short I am about 6 months into this just to get a 1975 ih150 up and driving after the previous owner threw in the towel about 3 yrs ago in strangecoach, nv. I paid $350 for her and have now spent about $750 since I dragged her home.
I am now ready to tackle the 304 engine which runs but has some oiling issues as well as 2 definite valve train problems. We pulled the valve cover on the driver side where the noise was coming from. I put the doc stewart chopped valve cover in place and ran the motor. #1 exhaust rocker was hardly moving. We, that is my buddy eldo gave the pushrods a twirl and found that #1 intake pushrod is bent a tad (maybe .25"). Oil draniback is fine. Oil is flowing along the rocker shaft. Inside the valve cover and the rocker area is fairly clean so it looks like she had good oil changes.
This motor is coming out for a rebuild based on the recent evidence uncovered and for some others as well.
Ok compression but sorta low 120 120 110 115 110 135 120 130
oil pressure about 15 at 2000rpm 22 at 2800rpm hot oil
leaky welch plugs under the intake manifold (coolant)
rusted out core pugs on the block beginning to leak
water pipe hold down on driver side missing and unable to replace because bolt head stuck against water pipe.
Tons of old blue rtv squeezed out of oil pan gasket, valve cover gaskets, water pump housing/timing cover gasket, oil filter adapter plate gasket and front oil seal. This alone is reason enough for a complete teardown because who knows what galleries are contaminated.
Most of the engine has been painted bumper chrome silver over dirt and grease.
More soon!!!
I am now ready to tackle the 304 engine which runs but has some oiling issues as well as 2 definite valve train problems. We pulled the valve cover on the driver side where the noise was coming from. I put the doc stewart chopped valve cover in place and ran the motor. #1 exhaust rocker was hardly moving. We, that is my buddy eldo gave the pushrods a twirl and found that #1 intake pushrod is bent a tad (maybe .25"). Oil draniback is fine. Oil is flowing along the rocker shaft. Inside the valve cover and the rocker area is fairly clean so it looks like she had good oil changes.
This motor is coming out for a rebuild based on the recent evidence uncovered and for some others as well.
Ok compression but sorta low 120 120 110 115 110 135 120 130
oil pressure about 15 at 2000rpm 22 at 2800rpm hot oil
leaky welch plugs under the intake manifold (coolant)
rusted out core pugs on the block beginning to leak
water pipe hold down on driver side missing and unable to replace because bolt head stuck against water pipe.
Tons of old blue rtv squeezed out of oil pan gasket, valve cover gaskets, water pump housing/timing cover gasket, oil filter adapter plate gasket and front oil seal. This alone is reason enough for a complete teardown because who knows what galleries are contaminated.
Most of the engine has been painted bumper chrome silver over dirt and grease.
More soon!!!

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