I have a 79 sii, with an 350 sbc, with the remaining drive train stock. (727, d20, d44's front and rear with 3.07's). I recntly had the transmission filter and fluids replaced, without a flush, and I had requested that the mechs do a band adjustment as prescribed by mm on the sticky. I even wrote the instructions down.
After the repair the trans did behave differently. If I start off slow, pulling away the trans seems to go thru 1st and 2nd pretty quick and there are no issues. Under hard acceleration, pulling away from a stop light or merging into traffic, the trans would get out of 1st quick (about 10-15mph), then the rpms would go up and the trans would 'let go' there doesnt seem to be any pulling at all until third, then all would be normal. Sometimes under the same hard accel, when it shifts out of first into second, the whole vehicle would shudder, like going over a rumble strip at 60 and second would kinda pull. Then on into third and everything seems to work fine.
After looking underneath, the amount of grease/crap on the band adjustment stud leads me to believe it wasnt done
, at least on that one. The one inside the pan -the easy one to get too- maybe. Before the visit to the garage, the trans would shift more like a manual, with definite shifts felt, and second would pull all the way to almost 2300 rpm/50 mph before deciding to move to third. Could this be one band tightened and another not, or maybe one band is toast. I have a new shifter cable coming in, so that will be the first thing towards a cure. I'll prob do-redo the band adjustment exercise as well.
Any thoughts? Should I sell a kidney
to get ready to get this thing fixed proper?
Thanks
After the repair the trans did behave differently. If I start off slow, pulling away the trans seems to go thru 1st and 2nd pretty quick and there are no issues. Under hard acceleration, pulling away from a stop light or merging into traffic, the trans would get out of 1st quick (about 10-15mph), then the rpms would go up and the trans would 'let go' there doesnt seem to be any pulling at all until third, then all would be normal. Sometimes under the same hard accel, when it shifts out of first into second, the whole vehicle would shudder, like going over a rumble strip at 60 and second would kinda pull. Then on into third and everything seems to work fine.
After looking underneath, the amount of grease/crap on the band adjustment stud leads me to believe it wasnt done

Any thoughts? Should I sell a kidney

Thanks