Danny Phillips
Member
Happy holidays everyone. I just reinstalled the 727 in my 74 Scout II after resealing it. When I fired it up after refilling it doesn't want to go into gear and when I shut it down it pukes oil out the dipstick tube. I put a new seal in the pump for the torque converter and new gasket and o ring on the pump. I filled the torque converter half full and then reinstalled it on the pump and verified it was engaged to the pump tabs. I had to slide it forward about 1/2" - 5/8" to bolt it to the flex plate. I also did the vent relocation and adjusted the bands. Anybody have any ideas before I have to remove it again? Thanks, Danny
Last edited: